ULTRA-FLO System Slashes Deviated Well Costs

ULTRA-FLO System before and after photosJJ Tech’s Innovative Solutions

Reliable, cost saving ULTRA-FLO System installed in shallow deviated wellbore increases production and slashes workover costs.

Objectives:
Maintain production rate of 250 bbls formation fluid / day
Increase Profitability of Well by Eliminating:
• Rod Cut Tubing
• Parting of Rods
Decrease Down Time Loss of Production

Results:
Increased production from 250 to 300 bbls / day
(20% increase)

No moving parts down hole eliminates the possibility
of tubing damage from rod wear (and there are no rods to part).

Download PDF for complete study

View D-35 ULTRA-FLO  Skid Diagram

Well Technical Data
Formation: Tuscaloosa
Pump Depth: 2846′
Perforations: 2880-2884′
Tubing Pressure: 880 psi
Downhole Rate: 780 bbls / day
Return Rate: 1100 bbls / day
Horsepower Used: 14
Casing Size: 5-1/2″
Tubing Size: 2-7/8″

JJ Tech 2.8 Jet Pump  Data
• Production up to 4500 bpd
• Conventional oil producing
• Can be run on 2.375 Tubing or larger
• Fits inside 4.5 casing and up
• Carrier retrieved by
reverse circulation or wire line